Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study

Detalhes bibliográficos
Autor(a) principal: Moreira, Miguel Ângelo da Cunha
Data de Publicação: 2021
Tipo de documento: Dissertação
Idioma: eng
Título da fonte: Repositório Científico de Acesso Aberto de Portugal (Repositórios Cientìficos)
Texto Completo: http://hdl.handle.net/10773/33706
Resumo: This work was developed as part of a curricular internship at Gestamp Aveiro, to reduce maintenance costs associated to the hot stamping production line. For the development of this report, an in-depth study of the entire production line was carried out (from the entry of raw material in the process to the exit of the final part), to identify the possible existing problems. These problems were related to early wear or repetitive equipment failures. The causes and consequences of these failures were investigated. The impact of each of the problems was studied to access which of those were to be worked on. The selected criteria were the percentage of the maintenance budget each represented. Research to implement new solutions and improvements carried out by the company were also analysed. The areas identified as most relevant were the wear of ceramic rollers in the kiln/furnace and its implications, the excessive wear of the blank referencing presses and the excessive contamination of the shop floor by metallic dust from the laser cutting process, with special impact on the laser tool head’s components. Then, a research was conducted to discover and propose improvements, to eliminate or minimize the problems identified and to implement those proposals. Criteria were sought for the evaluation of these proposals and the results were analysed. Due to external factors, not all proposals or solutions were applied. Therefore, a plan was developed for their implementation and subsequent analysis and evaluation of their results. Revisions to preventive maintenance plans were made and an internal procedure was developed as part of the improvement propositions. In conclusion, the main objectives of this work were achieved and considering all proposed solutions, significant costs reduction was achieved. Future research and work were proposed to proceed and improve some of the problems identified in this thesis.
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spelling Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case studyHot stampingCeramic rollersMechanical pressesHydraulic pressesIndustrial furnaceLaser trimmingLaser referencing black markingPreventative maintenanceCost reductionProcess optimizationThis work was developed as part of a curricular internship at Gestamp Aveiro, to reduce maintenance costs associated to the hot stamping production line. For the development of this report, an in-depth study of the entire production line was carried out (from the entry of raw material in the process to the exit of the final part), to identify the possible existing problems. These problems were related to early wear or repetitive equipment failures. The causes and consequences of these failures were investigated. The impact of each of the problems was studied to access which of those were to be worked on. The selected criteria were the percentage of the maintenance budget each represented. Research to implement new solutions and improvements carried out by the company were also analysed. The areas identified as most relevant were the wear of ceramic rollers in the kiln/furnace and its implications, the excessive wear of the blank referencing presses and the excessive contamination of the shop floor by metallic dust from the laser cutting process, with special impact on the laser tool head’s components. Then, a research was conducted to discover and propose improvements, to eliminate or minimize the problems identified and to implement those proposals. Criteria were sought for the evaluation of these proposals and the results were analysed. Due to external factors, not all proposals or solutions were applied. Therefore, a plan was developed for their implementation and subsequent analysis and evaluation of their results. Revisions to preventive maintenance plans were made and an internal procedure was developed as part of the improvement propositions. In conclusion, the main objectives of this work were achieved and considering all proposed solutions, significant costs reduction was achieved. Future research and work were proposed to proceed and improve some of the problems identified in this thesis.O presente trabalho foi desenvolvido no âmbito de um estágio curricular na Gestamp Aveiro, com o principal objetivo de reduzir os custos de manutenção associados à linha de produção de estampagem a quente. Para a execução deste relatório foi feito um estudo profundo de toda a linha (desde a entrada da matéria-prima no processo até ao término da peça final), com o objetivo de identificar o maior número possível de problemas existentes, relacionados com desgaste precoce ou falha repetitiva dos equipamentos. Investigaram-se as causas e consequências dessas falhas. De seguida, foi avaliado o impacto de cada um dos problemas identificados, sendo o critério a percentagem do orçamento de manutenção que representavam. Também foram analisadas tentativas de melhoria e outras investigações realizadas pela própria empresa. As áreas de atuação catalogadas como mais relevantes foram o desgaste dos rolos cerâmicos no forno e as suas implicações, o desgaste excessivo das prensas de referenciação dos formatos e a contaminação excessiva do chão de fábrica por pó metálico, proveniente do corte laser, com especial impacto no desgaste dos componentes da cabeça de corte laser. Após a análise e avaliação preliminar, foram propostas e implementadas melhorias para eliminar ou minimizar os problemas identificados. Procuraram-se critérios para avaliar estas propostas e analisaram-se os resultados obtidos. Devido a fatores externos, nem todas as propostas foram aplicadas, sendo que se concebeu um plano de implementação para posterior análise e avaliação dos seus resultados. Foram feitas propostas de revisão dos planos de manutenção preventiva e desenvolveu-se um procedimento interno, como parte das propostas de melhorias. Em conclusão, os objetivos principais propostos neste trabalho foram concluídos com sucesso, resultando poupanças significativas nos custos de operação da empresa. Foram identificados e propostos trabalhos futuros que procedem a este trabalho desenvolvido.2022-04-20T12:19:27Z2021-07-23T00:00:00Z2021-07-23info:eu-repo/semantics/publishedVersioninfo:eu-repo/semantics/masterThesisapplication/pdfhttp://hdl.handle.net/10773/33706engMoreira, Miguel Ângelo da Cunhainfo:eu-repo/semantics/openAccessreponame:Repositório Científico de Acesso Aberto de Portugal (Repositórios Cientìficos)instname:Agência para a Sociedade do Conhecimento (UMIC) - FCT - Sociedade da Informaçãoinstacron:RCAAP2024-02-22T12:04:50Zoai:ria.ua.pt:10773/33706Portal AgregadorONGhttps://www.rcaap.pt/oai/openaireopendoar:71602024-03-20T03:05:03.815585Repositório Científico de Acesso Aberto de Portugal (Repositórios Cientìficos) - Agência para a Sociedade do Conhecimento (UMIC) - FCT - Sociedade da Informaçãofalse
dc.title.none.fl_str_mv Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
title Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
spellingShingle Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
Moreira, Miguel Ângelo da Cunha
Hot stamping
Ceramic rollers
Mechanical presses
Hydraulic presses
Industrial furnace
Laser trimming
Laser referencing black marking
Preventative maintenance
Cost reduction
Process optimization
title_short Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
title_full Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
title_fullStr Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
title_full_unstemmed Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
title_sort Maintenance cost reduction and process optimization of the Hot Stamping line: Gestamp Aveiro case study
author Moreira, Miguel Ângelo da Cunha
author_facet Moreira, Miguel Ângelo da Cunha
author_role author
dc.contributor.author.fl_str_mv Moreira, Miguel Ângelo da Cunha
dc.subject.por.fl_str_mv Hot stamping
Ceramic rollers
Mechanical presses
Hydraulic presses
Industrial furnace
Laser trimming
Laser referencing black marking
Preventative maintenance
Cost reduction
Process optimization
topic Hot stamping
Ceramic rollers
Mechanical presses
Hydraulic presses
Industrial furnace
Laser trimming
Laser referencing black marking
Preventative maintenance
Cost reduction
Process optimization
description This work was developed as part of a curricular internship at Gestamp Aveiro, to reduce maintenance costs associated to the hot stamping production line. For the development of this report, an in-depth study of the entire production line was carried out (from the entry of raw material in the process to the exit of the final part), to identify the possible existing problems. These problems were related to early wear or repetitive equipment failures. The causes and consequences of these failures were investigated. The impact of each of the problems was studied to access which of those were to be worked on. The selected criteria were the percentage of the maintenance budget each represented. Research to implement new solutions and improvements carried out by the company were also analysed. The areas identified as most relevant were the wear of ceramic rollers in the kiln/furnace and its implications, the excessive wear of the blank referencing presses and the excessive contamination of the shop floor by metallic dust from the laser cutting process, with special impact on the laser tool head’s components. Then, a research was conducted to discover and propose improvements, to eliminate or minimize the problems identified and to implement those proposals. Criteria were sought for the evaluation of these proposals and the results were analysed. Due to external factors, not all proposals or solutions were applied. Therefore, a plan was developed for their implementation and subsequent analysis and evaluation of their results. Revisions to preventive maintenance plans were made and an internal procedure was developed as part of the improvement propositions. In conclusion, the main objectives of this work were achieved and considering all proposed solutions, significant costs reduction was achieved. Future research and work were proposed to proceed and improve some of the problems identified in this thesis.
publishDate 2021
dc.date.none.fl_str_mv 2021-07-23T00:00:00Z
2021-07-23
2022-04-20T12:19:27Z
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url http://hdl.handle.net/10773/33706
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